HAR2011
Structural
- Nov 18, 2011
- 5
Hi,
A new monorail beam after load testing to rated service load got a 1/2" permamnent deformation at the center. It deflected overall 3/4" at the center and then after removal of the load went back 1/4". The span is 14 ft. The beam has got 1/2" thk. plates welded to the top & bottom flanges over the entire span. Assuming that the design of the beam is adequate for strength and deflection (span/450 limit) for the load specified, could there be any other reason for this initial deformation?
A new monorail beam after load testing to rated service load got a 1/2" permamnent deformation at the center. It deflected overall 3/4" at the center and then after removal of the load went back 1/4". The span is 14 ft. The beam has got 1/2" thk. plates welded to the top & bottom flanges over the entire span. Assuming that the design of the beam is adequate for strength and deflection (span/450 limit) for the load specified, could there be any other reason for this initial deformation?