SHOULD BE LOW FLOW OPERATION.
YOU WILL ANALIZE WHY DESIGN SAYS 875MTERS BUT YOU HAVE 1025M.
IT IS 150METERS MORE.
WHAT COMPONENT OVERPRESSURE THE SYSTEM?.
ANY LOW PIPING DIAMETER, HIGH PIPING LENGTH, HIGH STATIC HEIGHT, FILTER, CONTROL VALVE, ETC.
SECOND, YOU SHOULD ANALYZE VALVE CONTROL OPERATION, LOGIC CONTROL AND VALVE SPECIFICATION, IF VALVE CONTROL IS NEAR TO BE IN CLOSE POSITION SO PUMP TENDS TO RUN IN HIGH PRESSURE/LOW FLOW POINT.
IF YOUR VALVE IS ALWAYS IN OPEN POSITION, YOU SHOULD KNOW HOW MUCH LOSS OF PRESSURE IT PRODUCE.
SO YOU WILL HAVE SOME OPTIONS, CHANGE LOGIC CONTROL ON CONTROL VALVE OR USE/INSTALL RECIRCULE LINE ON DISCHARGE PIPE.
SOME LOGIC CONTROL LIKE CONSTANT LEVEL ON SUCTION TANK ALWAYS MADE THIS KIND OF PROBLEM.
PLEASE INDICATE TYPE OF MOTOR BEARING, IT IS VERY IMPORTANT.
I THINK YOUR MOTOR IS NEAR TO 1500 HP, SO MOTOR MANUFACTURER WILL USE FRICTON SLEEVE BEARINGS. IN THIS CASE YOU SHOULD CHECK IF MAGNETIC CENTER IS CORRECTED POSITION BY COUPLING, IS THAT IS THE PROBLEM YOU HAVE TO MOVE THE MOTOR. BUT IF MOTOR BEARING IS NON-CONTACT BEARING AND IS HOT YOU SHOULD CHANGE TYPE OF OIL, SOME MOTOR MFG SUGGEST TO GO TO ISOVG68 WHEN YOUR OPERATION IS UNDER 82C AND GO WITH ISOVG100 WHEN IS ON THIS VALUE.
IT HELPS, PLEASE DOUBLE CHECK MY SUGGESTIONS.