zkz
Electrical
- Jul 3, 2008
- 21
Sir,
We have a 130MW generator (375RPM vertical hydro generator) in a powerhouse. When I took charge of Electrical Maintenance Engineer in that power house, I noted that the UGB vibration reading channel of Vibration monitor of that unit was found blocked. I also found that the LGB vibration channel and TGB vibration channel are in service . I enabled UGB vibration channel and found that its value is higher than other two channels. At rated RPM in unexcited mode, the unit showed the following values:
TGB: 2.2 mils; LGB: 1.6mils; UGB: 6.0 mils.
When the unit was excited, the UGB vibration increased to 7.0mils.
Some engineers in that powerhouse said me that UGB vibration alone can not increase without increase in vibrations of LGB and TGB. They explained that UGB channel was showing 'abnormal' values only because of vibration monitor fault and not actual vibration. That is why they blocked that channel in order to avoid unnecessary tripping. I checked UGB vibration with another portable vibration measuring equipment and confirmed that UGB vibration is high.
We are planning to carry out rotor balancing of the unit. We have already checked the tightness of rotor pole keys and wedges. Checked 'centering' (eccentricity) of sliprings with the help of dial gauges. Checked maximum travel of shaft (run out)at UGB end. The shaft diameter is 30 inches. Shaft clearance we got both in X and Y directions were 15mils. Eccentricity of sliprings were 20 mils.
I am kindly inviting your attention for valuable comments about the causes of high vibration and remedies.
Thanks in advance.
Regards,
appunni
We have a 130MW generator (375RPM vertical hydro generator) in a powerhouse. When I took charge of Electrical Maintenance Engineer in that power house, I noted that the UGB vibration reading channel of Vibration monitor of that unit was found blocked. I also found that the LGB vibration channel and TGB vibration channel are in service . I enabled UGB vibration channel and found that its value is higher than other two channels. At rated RPM in unexcited mode, the unit showed the following values:
TGB: 2.2 mils; LGB: 1.6mils; UGB: 6.0 mils.
When the unit was excited, the UGB vibration increased to 7.0mils.
Some engineers in that powerhouse said me that UGB vibration alone can not increase without increase in vibrations of LGB and TGB. They explained that UGB channel was showing 'abnormal' values only because of vibration monitor fault and not actual vibration. That is why they blocked that channel in order to avoid unnecessary tripping. I checked UGB vibration with another portable vibration measuring equipment and confirmed that UGB vibration is high.
We are planning to carry out rotor balancing of the unit. We have already checked the tightness of rotor pole keys and wedges. Checked 'centering' (eccentricity) of sliprings with the help of dial gauges. Checked maximum travel of shaft (run out)at UGB end. The shaft diameter is 30 inches. Shaft clearance we got both in X and Y directions were 15mils. Eccentricity of sliprings were 20 mils.
I am kindly inviting your attention for valuable comments about the causes of high vibration and remedies.
Thanks in advance.
Regards,
appunni