gosooners
Chemical
- Jul 21, 2007
- 15
Hi all experts,
Here is the situation in my gas processing plant :
MDEA of 50.5% is used to absorb CO2 and H2S with loading 0.37 m/m. I have corrosion problem in exit of lean/rich exchanger pipe to entry of the stripper(first 4 trays) and bottom of the tower. I have checked following analysis :
HSS(0.12-0.2 wt%)
Temperature in the reboiler : 250 F
Filtering system is working fine. But one think i noticed with modelling is high velocity(13 ft/sec) in the pipeline entering to stripper column. The tower operates at 9 psig. Control valve is at the ground level and vertical pipe of 75 ft goes to top of the stripper column. My model says high velocity in the vertical pipeline somewhere in the vertical pipeline after exiting from control valve.
There is no significant corrosion problem in L/R exchanger.
Corrosion in top of the tower and pipeline that enters to the tower is significant appx 80 mils/year. Right now we started temporary corrosion inhibitor solution. But still I am thinking high velocity is the factor of this problem.
Can you suggest me probable reason for this. I need quick suggestions for this.
thanks in advance for your suggestions.
Here is the situation in my gas processing plant :
MDEA of 50.5% is used to absorb CO2 and H2S with loading 0.37 m/m. I have corrosion problem in exit of lean/rich exchanger pipe to entry of the stripper(first 4 trays) and bottom of the tower. I have checked following analysis :
HSS(0.12-0.2 wt%)
Temperature in the reboiler : 250 F
Filtering system is working fine. But one think i noticed with modelling is high velocity(13 ft/sec) in the pipeline entering to stripper column. The tower operates at 9 psig. Control valve is at the ground level and vertical pipe of 75 ft goes to top of the stripper column. My model says high velocity in the vertical pipeline somewhere in the vertical pipeline after exiting from control valve.
There is no significant corrosion problem in L/R exchanger.
Corrosion in top of the tower and pipeline that enters to the tower is significant appx 80 mils/year. Right now we started temporary corrosion inhibitor solution. But still I am thinking high velocity is the factor of this problem.
Can you suggest me probable reason for this. I need quick suggestions for this.
thanks in advance for your suggestions.