joeh2o
Mechanical
- Jul 25, 2003
- 7
2 on 1 combined cycle plant. 2 7FA with ATS HRSG to an ABB reheat steam turbine. 4 years old.
Perfromed hot gas path inspection on both GT in October 2002. Noticed a drop in STG output. This was expected due to the lower TEG temperature after the inspection. In February of 2003 we had a limited STG overhaul involving reduction gear re-alignment, bearing inpection, gland steam modification, borescope and relocation of the excitation control module. We also installed new duct burners on both HRSGs. After we started up after this outage we noticed another step change in the STG output. Right now we are experiencing a loss of about 3 to 4 MW. The GTs are determined to be performing up to standards. A HRSG perfromance audit was performed by a company out of minnesota and found that the HRSGs were performing as they should. However trending shows that steam production in the HP and IP sections of the HRSG have decreased and the LP section steam production has increased. HP turbine exhaust pressure and temperatures are lower when compared to similar plant conditions. Also HRH steam pressure has decreased. While we are troubleshooting all we can think of is there any more input that some one could give me on what else to look at in order to track down this problem?
Perfromed hot gas path inspection on both GT in October 2002. Noticed a drop in STG output. This was expected due to the lower TEG temperature after the inspection. In February of 2003 we had a limited STG overhaul involving reduction gear re-alignment, bearing inpection, gland steam modification, borescope and relocation of the excitation control module. We also installed new duct burners on both HRSGs. After we started up after this outage we noticed another step change in the STG output. Right now we are experiencing a loss of about 3 to 4 MW. The GTs are determined to be performing up to standards. A HRSG perfromance audit was performed by a company out of minnesota and found that the HRSGs were performing as they should. However trending shows that steam production in the HP and IP sections of the HRSG have decreased and the LP section steam production has increased. HP turbine exhaust pressure and temperatures are lower when compared to similar plant conditions. Also HRH steam pressure has decreased. While we are troubleshooting all we can think of is there any more input that some one could give me on what else to look at in order to track down this problem?