Root cause analysis
Root cause analysis
(OP)
Hi everyone.
I would like to consult for a blower that was recently repaired? I would appreciate any help on this.
Attached document is my initial investigation of the blower and hopefully you may take time to read this. On the last pages of this presentation are only my suspicion. I haven't included the integrity of the Allen cap screws but would also send this for a shear test and tensile test for verification. This blower is driven by a 250hp motor/4160voltage. Blower speed is 1565rpm. I would really need any expert advice on this matter.
I would appreciate any help on this please.
Thank you very much.
Sincerely,
Whispair guy (fmcseals)
I would like to consult for a blower that was recently repaired? I would appreciate any help on this.
Attached document is my initial investigation of the blower and hopefully you may take time to read this. On the last pages of this presentation are only my suspicion. I haven't included the integrity of the Allen cap screws but would also send this for a shear test and tensile test for verification. This blower is driven by a 250hp motor/4160voltage. Blower speed is 1565rpm. I would really need any expert advice on this matter.
I would appreciate any help on this please.
Thank you very much.

Sincerely,
Whispair guy (fmcseals)
RE: Root cause analysis
RE: Root cause analysis
RE: Root cause analysis
RE: Root cause analysis
Given the very small gaps between the lobes in a roots blower, am not surprised this blower has failed in abrasive coal fines service. The roots blower I worked with many years ago was in plain (clean) combustion air delivery service. Wouldnt a centrifugal blower be a better choice here ( typically used in fines laden hot exhaust fumes service), or is the required dp of 9.2psi too much for a centrifugal option?
RE: Root cause analysis
It was caused by a machining error that introduced a stress concentration at the intersection of the input drive shaft and the rotor body. The alternating stress came from the belt drive which had been converted from V-belts to cog belts.
I suspect a problem with your belt drive that overstressed the connection between the drive shaft and the rotor: belt tension, eccentric sheave, belt alignment, etc.
Our machine also had various cracks that may have been unrelated to this particular failure.
Our lift gas blower experienced another failure when the inlet bag filters failed and catalyst dust plugged up the machine.
Johnny Pellin
RE: Root cause analysis
Thank you for taking time and sharing your thoughts about my project repair for Whispair Roots Blower.
I forgot to include in my report that on the 1st and 2nd trial during operation of this blower we decided not to couple the discharge port to the silencer and operate this with an open port just to inspect, feel, hear and see if the blower operates freely without any rubbing on the cylinder housings and lobes on each other. The cylinder body's maximum temperature reading was only 40Deg C and the drive end bearing temperature max was only 82 Deg C. The rest of the surfaces of the blower reads only 35 to 40 Deg C....so far it was perfectly operating until the they decided to shut it down in the evening as the central control noticed that there was a sudden drop of amperage during the night and decided to operate the parallel unit or back up unit. To which I don't know yet the time when they decided to couple the ports to the silencer and start conveying the fine coal on the downstream where at the moment how much time was it running while coupled to the silencer and a sudden drop of amperage is noticed.
I have inspected well all the components and parts where everything is without wear on the surfaces of the cylinder, lobes, bearing fits, bearing journals, drive and driven gears etc., that should occur if a rubbing or sudden jerk of operation would prove. Please see the attached photo for your references and videos during operation on an open port.
Those marks you may notice on the head plate are just nominal to very slight wear. I suspect this mark happened after the breakage of the Allen cap screws as it took us time to withdraw the unit from the skid base of the blower.
And yes Tugboat I don't have any explanation on the corrosion of the allen cap screws yet as of now. I will try to check this and view it with your perspective as it might help us gather more information.
Thank you for patiently reading my feedback. I am just new on this website and there are a lot of photos and videos I wish to share and would still need time to study how to navigate this page.
Awaiting for any more comments and will surely be appreciated.
Have a nice day!
RE: Root cause analysis
RE: Root cause analysis
For your case I would be very curious if the builder centered the rotor axially in the housing. The rotor should be set near the minimum clearance on the thrust bearing end and allowed to expand in the extra space at the axially free end. Centering the rotor could allow it to contact the housing opposite the thrust bearing at high operating temps.
The second issue I see is that the rotors get timed in the lead direction but not trailing. I have heard this cause some rattling during coasting as the rotors touch lightly.
RE: Root cause analysis
I wasn't able to measure the clearances prior to disassembly as I was directly worried if the drive shaft snapped like JJPellin said. But during the process we got a discovery of broken allen cap screws...
Yes we got the correct clearances prior to assembly before just like you mentioned but I am not sure of the timing of trailing and leading. Could you please enlighten me about this? From what I also remember is the timing were also synchronized well. I would appreciate your experience on this please.
RE: Root cause analysis
RE: Root cause analysis
RE: Root cause analysis
Thank you for any comments on this.
RE: Root cause analysis
Is it also possible that the back pressure due to blockade or restriction of flow can really snap all of the 14pcs Allen Cap Screws of the drive shaft and also ending up cracks on the body of the blower as well as gear head plate and drive head plate? I can't help but think of this problem due to my previous blower repair (a smaller model by 20% only) almost had an accident as operators forgot to open the valve for 1 to 2 minutes until one of the inspectors notice it and immediately shut down the machine then instructed the operators to open the valve. During this process we notice an immediate rise of temperature in the body of the blower. Could it be that this happened also to this bigger blower that we recently repaired?
Thank you everyone for your feedback.
RE: Root cause analysis
I notice also that the belt of the blower during operation has a higher tension than expected during my trial. I didn't mind it as I thought it was just normal. I think your theory is also one to consider. Operation would reason to me that it has been that way ever since and haven't any issue before so I would need a better and compelling reason to convince them of changing to cog belt.
Thanks again.
RE: Root cause analysis
RE: Root cause analysis
If your design does not have a relief valve it is easy to imagine you can exceed the casing structural load limit. you can calculate bolt shear stress applied from motor breakdown torque in a similar manner.
RE: Root cause analysis