Abeshaka
Civil/Environmental
- Jun 9, 2016
- 2
Wanted to see if any one has any idea the cause of the settlement seen in the trench zone. Background the trench is approx. 10 feet and 21 feet deep the ground water table is usually at 10-12 feet. dewatered every 50 feet to draw down the water table to 21 feet below grade, pipe 60" sewer pipe installed and encased in CLSM (2 feet above pipe) that that point was backfilled with Clayey Sand, 35percent passing #200 sieve, LL of 25 and PI of 11 Proctor around 121.8 @13.8, all fill was compacted to 90 percent or greater and 2to 5 percent above the optimum. Two feet of Type II compacted to 95 percent. and no problems were encountered.
When the dewatering was stopped and the groundwater levels raised up back to 10 to 12 feet below grade , 8 to 10 inches of settlement was observed in certain areas along the trench line?????
Any thoughts When we drilled borings the blow counts dropped of to 1 and 2 when we got close to the water and the fill above the water table ranged in 5 to 10 blows per foot (N60).
When the dewatering was stopped and the groundwater levels raised up back to 10 to 12 feet below grade , 8 to 10 inches of settlement was observed in certain areas along the trench line?????
Any thoughts When we drilled borings the blow counts dropped of to 1 and 2 when we got close to the water and the fill above the water table ranged in 5 to 10 blows per foot (N60).